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gum
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Degumming; Ramie;
Fibers; Swelling;
Sodium hydroxide;
Feasibility studies
Sari :
Proses degumming serat rami yang umumnya dilakukan di IKM pengolah rami
yaitu menggunakan natrium hidroksida (NaOH) pada konsentrasi relatif tinggi, suhu
100 derajat C dan waklu berkisar 6 jam, dilanjutkan pemberian zat, pelemas pada
suhu 50 derajat C untuk membantu penguraian serat. Dalam penelitian modifikasi
degumming serat rami metoda kimia, telah dilakukan melalui proses awal
sebelumdegumming dengan NaOH, untuk mendapatkan proses degumming yang
lebih efisien dan efektif. Proses awal dikerjakan dalam larutan asam dilanjutkan
dengan degumming dalam NaOH sehingga pemakaian NaOH relatif lebih sedikit
dengan waktu proses lebih singkat. Kondisi optimum proses dicapai pada saat
serat belum terhidrolisa, namun telah menggelembung (swelling),
sehingga gum pada serat akan mudah terdegradasi pada proses degumming.
Kondisi optimum degumming dibuktikan berdasarkan hasil uji kehalusan serat,
kekuatan tarik, mulur, modulus awal, dimensi serat, dan fotomikroskopi penampang
serat. Hasil uji optimum diperoleh pada konsentrasi asam sulfat 5 g/l dan NaOH6
g/l, yaitu kehalusan serat: 4.9 denier, tenacily : 7,27 g/denier, mulur : 3,5 % dan
modulus awal : 192,25 g/denier. Hasil analisa limbah cair pada modifikasi
proses degumming antara lain COD dan BOD relalif lebih kecil dengan pH
mendekati normal, dibandingdegumming tanpa proses awal. Dari tinjauan aspek
ekonomi diketahui bahwa modifikasi proses degumming ini memberjkan
penghematan bagi IKM meliputi waktu proses berkurang 50 %, bahan bakar
minyak tanah 60 % per hari dan tenaga kerja 50 %. Analisa tekno ekonomi dengan
asumsi bahwa proses degumming per hari sebanyak 400 kg serat rami China
grass dan harga jual serat stapel Rp 20.000/kg, maka untuk degumming tanpa
proses awal diperoleh laba sebesar 28 % per tahun dengan BEP 67 %, sedangkan
dengan harga jual yang sama untuk modifikasi proses degumming dibuktikan
dengan laba sebesar 35 % per tahun dengan BEP 58 %.
Abstrak : Degumming process for ramie fiber in SME usually has been being done by using
sodium hydroxide (NaOH) at high concentration, temperature at 100 degree C and
could be done for ahoul 6 hours, followed by addition of softening agent at the
temperature qf 50 degree C to make the fibers easier to separate individually. In
this research pretreatment was done before degumming of ramie fiber to get more
efficient and effective process. Pretreatment was done in acid solution and followed
by degumming process in sodium hydroxide solution so less sodium hydroxide
could be needed and less time of period for the process. The optimum condition
process had reached where the fiber had not been hydrolyzed yet, but had already
been swollen, so that gum content in the fiber could be easier to degrade during
degumming process. The optimum condition of degumming had been proved
based on the test results i.e. fiber fineness, tensile strength, elongation, initial
modulus, fiber dimension, and photomicroscopic of fiber cross section. The
optimum result was obtained by using 5 g/l of sulphuric acid and 6 g/l of sodium
hydroxide, i.e fineness: 4,9 denier, tenacity: 7,27 g/denier, elongation: 3,5 % and
initial modulus: 192,25 g/denier. The waste water characteristic showed that COO
and BOD value were lower with pH near normal as compare to degumming process
without pretreatment. The techno-economical aspect of modification degumming
method has indicated profitable for SME including : 50 % decreasing of processing
time, 60% daily of saving petroleum energy and 50 % decreasing of employer.
Analysis of economic aspect with the assumption of degumming process for 400 kg
china grass and the selling price qf staple fiber is Rp 20.000/ kg, so that for
degumming without pretreatment will gain benefit by 28% annually and BEP 67%,
but for the same selling price with modification degumming process will be proven
beneficial of 35 % annually and BEP 58%.