Liners Faliure

Embed Size (px)

Citation preview

  • 8/11/2019 Liners Faliure

    1/17

    Fr7AE Gas TurbinesDry Low-NOx Combustion System

    Operating Challenges in O&G Plants

    Atul W. Deshpande RasGasLuis A. Rojas RasGas

    V. Venkatachallam RasGasMustapha Chelghoum RasGas

  • 8/11/2019 Liners Faliure

    2/17

    Executive Summary:

    After a planned Shutdown and transfer valvereplacement, Propane unit -GT Fr7AE DLN1-started;

    Unit failed to transfer to pre-mix steady stateMode (PMSS) and Trip.

    05 Days of online troubleshooting using FishboneDiagram, to determine why the unit couldn

    tsustain on PMSS mode after several transfers.

    Visual inspection of the internal Combustionsystem reveal hardware damages.

    RCFA-PROACT Methodology used to investigateand find the causes of the damages.

  • 8/11/2019 Liners Faliure

    3/17

    Why DLN1 system on Gas Turbine andHow it works during Startup?

    The DLN-1 for FR7AE GT meet Qatar Ministry of environment (MOE)in terms of emission norms (NOx < 25 ppm).

    Axial AirCompressor

    Airinlet

    PowerTurbine

    Purge AirFlangeConnection toPurge Valves

    Vent

    PurgeValve-1

    PurgeValve-2

    VGC-3

    FUELGAS

    SRV

    VGC-2

    VGC-1

    PrimaryFuelManifold

    Transfer/ PurgeManifold

    Secondar y FuelManifold

  • 8/11/2019 Liners Faliure

    4/17

    Fishbone Diagram for Online Troubleshooting

  • 8/11/2019 Liners Faliure

    5/17

    Combustion Inspection Findings

    Carbone DepositsOn Primary andSecondary Nozzles

    ThermalDamage

  • 8/11/2019 Liners Faliure

    6/17

    Combustion Inspection Findings:Combustion Liner No 5: Major damage

    Liner #5 CrackedCircumferentially

    Material MeltedDown Insidethe Liners.

    Liners LateralCracks

    Liner CapsDeformation

    Loss of Material

  • 8/11/2019 Liners Faliure

    7/17

    Combustion Inspection Findings:Combustion Liner No 4: Major damage

    Liner #4 CrackedCircumferentially

    Missing PieceNear Hula Seal Cracks and

    LateralMovement

    3 Liner CapsDeformedDownward

  • 8/11/2019 Liners Faliure

    8/17

    Root Cause Failure Analysis RCFAEvent Diagram:

  • 8/11/2019 Liners Faliure

    9/17

    Investigations..1Control System Trends.

    Fuel gas Pressure Fluctuations before the event

  • 8/11/2019 Liners Faliure

    10/17

    10

    Investigations ..2Control System Event Trends during transfer

    Spike in Compressor Pressure &Exhaust temperature

  • 8/11/2019 Liners Faliure

    11/17

    11

    Investigations..3Purge Air Connection on Wrapper

    Side View of Wrapper

    Purge AirConnectionTo Wrapper

    2

    4

    3

    5

    EndView

    Gas

    Air

    Liner DamageArea

    Purge Air Connection on Wrapper Close to combustion can #4&5

  • 8/11/2019 Liners Faliure

    12/17

    12

    Investigations..4Purge Valve installation

    Same SAP number Normally closeactuator & Normally Open actuator

    Ball closes opposite toseat leaving wide gap

    in closed condition

    Closing opposite to seat/Incorrect SAP material number

  • 8/11/2019 Liners Faliure

    13/17

    Investigations..5Fuel Gas System.

    13

    Selexol draineddaily

    53 - C010

    SELEXOL Absorber

    LC

    53 - V010

    SELEXOL KO DRUM

    Unit 53 Battery Limit

    93 - V121

    FG MIXING DRUM

    EFG FFF

    93 - E122

    ~50 C

    ~42 C

    FG scrubber& strainer skid

    56 - Y004

    FG Valve Skid(56 - Y002)

    Gas Turbine (56 - KT004)

    FG scrubber& strainer skid

    56 - Y003

    FG Valve Skid(56 - Y001)

    Gas Turbine (56 - KT001)

    LeanSELEXOL

    solvent

    Rich

    LC LC

    53 - V010

    SELEXOL KO DRUM

    Unit 53 Battery Limit

    93 - V121

    FG MIXING DRUM

    EFG FFF

    93 - E122

    ~50 C

    ~42 C

    FG Filters 56 - Y004

    FG Valve Skid(56 - Y002)

    Gas Turbine (56 - KT004)

    FG Filters

    56 - Y003

    FG Valve Skid(56 - Y001)

    Gas Turbine (56 - KT001)

    LeanSELEXOL

    solvent

    RichSELEXOL

    solvent

    Regen gas fromdehydration unit

    (Unit 53)

    FFF (duringstartup)

    ~65 C

    ~48 kNm3/hr

    Excess gas to fuelgas header

    ~15 kNm3/hr

    ~15 kNm3/hr

    Sour Gas Flare

    Fuel gas strainer

    Filters Specification 0.3m for solid &

    liquid removal, existing 3m for solidonly .

    Mixing drum not a knock outdrum (no demister) Upstream demisters noteffective

  • 8/11/2019 Liners Faliure

    14/17

    RCFALogic Tree (1)

    14

    Hardware damagedue to uncontrolled

    combustion

  • 8/11/2019 Liners Faliure

    15/17

    RCFALogic Tree (suite)

    15

    Main Cause:Backflow of Fuel gas

    through purge lineContributing Fact:

    Liquid accumulation due toinadequate Filtration and

    piping lay out

    Main Cause:Backflow of Fuel gas

    through purge line

    Main Cause:Backflow of Fuel gas

    through purge lineContributing Fact:

    Liquid accumulation due toinadequate Filtration and

    piping lay out

    Contributing Fact:Liquid accumulation due to

    inadequate Filtration andpiping lay out

  • 8/11/2019 Liners Faliure

    16/17

    16

    RCFARecommendations

    Work Management:

    Change SAP material code for the purge valve actuator. Develop Purge Valve Installation Procedure. Time based purge valve replacement.

    Engineering Design:

    Upgrade purge valves, actuators, solenoid. DLN mode transfer software modification. Upgrade fuel gas filtration system & DLN valve skid layout. Upgrade demisters of Selexol Absorber & mixing drum. Install Combustion Dynamics Monitoring system for allFrame 7 DLN Gas turbines.

    All recommendations have been implemented.

  • 8/11/2019 Liners Faliure

    17/17

    17

    Questions?