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    Abstract

    In order to reduce the heat loading in the Tilden Mine kilns caused

    by burning coal, which in turn resulted in rapid and significant build-up

    on the kiln lining, internal carbon was added to the green ball prior to

    balling. Intensive laboratory testing led to three short-term full-scale

    plant tests that were successfully conducted. Appropriate

    environmental permits were obtained to allow Tilden to use internal

    carbon on a continuous basis. Findings concerning carbon addition

    rates, reductions in coal use, build-up reductions, fired pellet quality,

    and environmental issues will be discussed.

    Introduction

    This paper discusses the successful use of internal fuel (coke

    breeze) during the production of hematite fluxed pellets on the two

    grate-kiln systems at the Tilden Mine. It is believed by the authors

    that this is the first time that internal fuel has been used successfully

    on grate-kiln systems in North America.

    Cleveland-Cliffs, Inc is the largest supplier of iron ore products to

    the North American steel industry. Subsidiaries of the company

    manage and hold equity interest in five iron ore mines in North

    America. These are the Empire and Tilden Mines in Michigan, the

    Northshore and Hibbing Taconite (Hibtac) mines in Minnesota, and

    the Wabush Mine in Labrador and Quebec, Canada.

    The Companys wholly owned subsidiary, Cliffs Mining Services

    Company (CMSC), operates a Research Laboratory in Ishpeming,Michigan. It also manages Engineering Services in Ishpeming. Both

    Engineering Services and the Research Laboratory service all five

    mines

    Reason for Internal Carbon Study

    Kiln ringing and build-up is a very significant and expensive

    problem at Tilden when producing hematite fluxed pellets with 100%

    coal firing. Straight grate indurating systems processing hematite

    have used internal fuel to improve pellet quality, provide intimate heat

    input and reduce heat consumption. Internal fuel additions generally

    have approximated the quantity of heat evolved if the concentrate was

    magnetite. It was theorized that if an internal fuel could replace the

    heat provided by magnetite oxidation, the amount of heat required to

    be supplied by the kiln burner would be significantly reduced. Tilden

    experiences significantly less kiln build-up when processing

    magnetite concentrate. To evaluate this concept, a series of pot

    grate-batch kiln tests were conducted with Tilden hematite fluxed

    concentrate with and without internal coke breeze addition. The pot

    grate-batch kiln tests were successful, which led to a successful three

    day plant test on Units 1 and 2 at Tilden.

    Pot Grate Kiln Test Summary

    Pot grate-batch kiln tests were conducted at Cliffs Technology

    Center without internal fuel and at 0.5 and 1.0% addition levels. For

    most of the tests the coke breeze was added to concentrate slurry and

    pressure filtered before bench balling. Two of the tests had the coke

    breeze added dry and mixed with the bentonite before bench balling.

    The 1% internal coke breeze addition improved green ball,

    preheat pellet, and fired pellet physical quality, except for fired pellet

    compression strength, which was reduced slightly. It also, improved

    pellet LTB and maintained reducibility. The total time required in

    preheat was reduced by 0.44 minutes, which indicates that Tilden

    may also get a slight production increase with internal coke breeze.

    Bench balling with coke breeze was visually much easier and created

    very little seed material compared to baseline balling. This was thecase with either slurry or dry addition. With hematite fluxed pellets a

    1% internal fuel addition rate could reduce coal burning in the kiln by

    around 35% or 7 ST per hour. Because of the success of the pot

    grate kiln test program, Tilden ran a four-day plant test on both units

    starting on October 1, 2001.

    Plant Test Summary

    On day shift on Monday, October 1, Tilden began introducing

    coke breeze into the plant. The coke breeze was ground in the 1B

    1 Copyright 2003 by SME

    2003 SME Annual MeetingFeb. 24-26, Cincinnati, Ohio

    Preprint 03-078

    INTERNAL CARBON ADDITION DURING HEMATITE FLUXED PELLET PRODUCTION AT THE TILDEN MINE

    M. J. HanninenT. E. SeppanenC. R. Sundberg

    Cliffs Mining Svcs Co.Ishpeming, MI

    P. J. SuardiniTilden Mining Co. L. C.

    Ishpeming, MI

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